Jump to content

D-5 okay for Crown seal?


Recommended Posts

I am finding that I have some resistance when pushing the crown back in to wind it closed on an ETA 2824-2. I think that the seal under the crown might be a little dry and that some oil might do the trick. Will a few drops of D-5 be suitable to put on the seal or is grease better...or something else? I seem to use D-5 as my goto magic all purpose oil :-) 

Cheers

John 

 

 

 

Link to comment
Share on other sites

Solution, I think, well seems to have resolved the issue was a little KT-22 around the thread and on the seal. 

 

As I suspected, D-5 didn't do much at all. 

Edited by John Hondros
Link to comment
Share on other sites

11 hours ago, John Hondros said:

I am finding that I have some resistance when pushing the crown back in to wind it closed on an ETA 2824-2. I think that the seal under the crown might be a little dry and that some oil might do the trick. Will a few drops of D-5 be suitable to put on the seal or is grease better...or something else? I seem to use D-5 as my goto magic all purpose oil :-) 

Cheers

John 

 

 

 

A silicone grease of some sort should be used. Oil could seep & contaminate.

Link to comment
Share on other sites

Thank you for the info. I did wonder whether the oil would seep and contaminate.  It makes intuitive sense that grease is what should be applied to rubber seals/o-rings. I should have trusted my gut instinct I guess 

 

Thanks! 

:)

Edited by John Hondros
Link to comment
Share on other sites



  • Recently Browsing

    • No registered users viewing this page.
  • Topics

  • Posts

    • It looks like the canon pinion function is part of this great wheel. The pinion nearest the clip runs the minute wheel on the dual side. The pinion nearest the wheel is driven by a small wheel from under the setting lever cover plate that engages in hand setting position.    So when assembled the crown was driving the whole great train. Does this mean the pinions are too tight? Should I attempt to disassemble this great wheel and lubricants?
    • Picking up this side-tracked post again as I just removed a balance staff of a 1920's Omega (35,5L-T1) I was impressed by the way @Delgetti had his setup when he had to change out a balance-staff (https://www.watchrepairtalk.com/topic/28854-new-balance-staff-not-riveting-to-balance/page/2/#comment-244054 Not only that, but also the idea of removing the seat first before punching the staff out from the seat-side, avoiding the whole discussion of the rivet yes/no enlarging the hole. I didn't have the fancy clamps & tools Delgetti has, so I used my screw-head polishing tool. Initially I used #1500 grit diamond paste on the steel wheel, which kinda worked, but very slow. I changed to #800 grit diamond paste, which worked better, but still slow. Then I glued #240 sanding paper to the steel disk; That worked and the disk was hand-driven. Once close to the balance wheel, I took the sanding paper off and continued with #800 diamond paste. One can only do this when the balance wheel sits true on the staff and has no "wobble". I went on grinding until I saw some diamond paste on the rim of the balance wheel. This was as far as I could grind and it seemed that there wasn't much left of the seat. Carefully, with my staking set, I knocked the staff from the seat-side out. Turns out that the thickness of the seat left, now a small ring, was only 0.1mm. The balance wheel hole is in perfect shape and no damage done to the wheel at all. Of course, if the wheel has a "wobble" or isn't seated true on the balance staff, you can't get as close and there will be more left of the seat. In my case, it worked perfect 🙂 I'm very happy how this method worked out ! 😊  
    • As is tradition, one step forward, two steps back. Got the board populated and soldered into place without any issues.   But no hum. So I started testing the coils with an ohmmeter. I got 5.84k ohms across D1 (from red to red in the picture below), which is as expected. But I'm getting an open circuit for the other drive coil and feedback coil, D2 and F1 (from green to each of the two yellows).   Since the movement was working with my breadboard setup, it implies I somehow broke the connection between the coils and the solder lugs. They're all the way at the bottom of the lugs, but maybe the heat migrated down and broke the connections? I guess it's possible it happened while cleaning the flux off, but I used a soft artist's brush and isopropyl alcohol. I did a lot of high magnification examination, and I don't see any issues, but let me know if you see anything I missed or if you can think of anything else I should check.
    • 1947 NOS Ambassador 'C'. Actually, the case came without the movement so the movement isn't NOS, but she sure is pretty.
    • Hi attached is the AS 20XX. Service sheet although there is no 2063 mentioned it may be of some use to you AS_AS 2060,1,2,6,4,6.pdf
×
×
  • Create New...