Jump to content

Hermle 340-020 slowing down as days go by


Recommended Posts

Have a 1976 Hermle 340-020. It ran for maybe 10 years back then and then stopped. It sat unused until a few months ago when I decided to look into getting it running again. I cleaned the pivot points and oiled them. Then cleaned the escapement with a artist brush and a solvent. Then oiled it. The clock is now running. 

 However, I have been tracking its accuracy. What I see is that after winding it runs fast but slows as the days go by. For example.

1 day after winding- gained 30 sec in 24 hours. 

2 days after winding- gained 20sec in 24 hours.

3 days after winding- lost 28sec in 24 hours

4 days after winding- lost 1min 45 sec in 24 hours

5 days after winding-  lost 2min 30 sec in 24 hours.

Is this normal? If not, what could be causing this drop off in regulation?

Thanks

Link to comment
Share on other sites

Hi welcome to the forum. The issue you are experiencing with the clock is typical of a clock that needs servicing with a high probability that bushes need replacing. When fully wound this issue is overcome but as the mainspring unwinds there is less power and the clock slows.Looking at the barrel barrel bushes would be a good starting point 

Edited by clockboy
  • Like 1
Link to comment
Share on other sites

Thank you for your introduction and welcome to this friendly forum.

We all look forward to your contributions and continued involvement. 

We like new members to make an introduction before posting. 

Is it a pendulum movement or floating balance? As clockboy has said what the problems could be I totally agree. You will need to remove the springs from the barrels so you will need a clock mainspring winder, springs can become week and will not work properly due to lack of oil and dirt. Photos would be good we might be able to spot something. Please make sure they are clear , both plates and the inside of the movement. 

  • Like 1
Link to comment
Share on other sites

This movement has a floating balance. It is a mantel clock. I took some pictures as I did my work just to make sure I could put it back together. They are not extensive or the best quality. I don't want to take the movement out again to get more pictures, at this time, because it seems every time I do, it acts different when put back in the cabinet. I want to study its behavior for a while.

I have considered buying a new movement, but it bothers me that although it was made 38 years ago, it only ran for maybe 10 of those years. In terms of run time, its not that old. And then there is the concern that I might pay $400 for a new one and it has the same accuracy limitations.20240310_171223.thumb.jpg.b45b8c622ddf99ec280fd134c422c4f1.jpg20240128_184954.thumb.jpg.ba79ef0446a1ee42839f0d480eec4fea.jpg

Link to comment
Share on other sites

The floating balance should be oiled, just a tiny drop of watch oil at the top jewel so it runs down the wire. You really need to get to the mainsprings as they are the source of the power.  

  • Like 1
Link to comment
Share on other sites

I have a copy of the Hermle service manual. It lists the lubrication point with a note saying the bearings on the old floating balance unit should not be lubricated. So I did not do it.

image.png.715649cd56c85338d7881abbec593114.png

This is part of the discussion of the main spring in the manual. I get the feeling you are right about the main spring needing attention. Although I am a little (a lot) afraid to take down the movement that far. Will likely end up buying new movement to get a functional clock and then experiment with the old movement just for the fun and challenge of it. 

image.png.d660317113dbafec655fbc02922b5cae.png

Link to comment
Share on other sites

Well I have around 30 years experience restoring clocks and watches. I have serviced many floating balance movements and always added a tiny drop of oil to the floating balance,not only Hermle but Smiths it improves the rotation of the balance and I have never had any come backs. 

  • Like 2
Link to comment
Share on other sites

On 3/25/2024 at 7:59 PM, DirkP121 said:

1 day after winding- gained 30 sec in 24 hours. 

2 days after winding- gained 20sec in 24 hours.

3 days after winding- lost 28sec in 24 hours

4 days after winding- lost 1min 45 sec in 24 hours

5 days after winding-  lost 2min 30 sec in 24 hours.

Is this normal? If not, what could be causing this drop off in regulation?

Thanks

This is a nice table, but it misses the main parameter - the amplitude of balance oscillations.

As You say the movement behaves differently every time when something done to it - I will suggess the amplitude is not good and this may be because the balance/escapament interaction is not well adjusted. The 'guard pin' there is different compared to 'normal' movements. It is a little capricious to adjust, it has not to touch the balance in any of it's position

Edited by nevenbekriev
Link to comment
Share on other sites

nevenbekriev-

Thank you for commenting. Every time I get a comment, it triggers new thoughts and insight.

You "liked" the table but asked about amplitude. Are you wondering what a table with amplitude verse days might look like? How would you measure amplitude? In degrees of rotation of the floating balance wheel?

You mentioned the guard pin. Is this the pin you are referring too? If so, are you concerned about it hitting what is the safety roller in the diagram 2?

image.png.900d40f17190690e93c690d244fae39b.png

These comments have got me doing more research. I found a document.

Hermle Floating Balance Summary of Inspection, Diagnosis, Cleaning and Repair Procedures … ..prepared by David Robertson

It states

Check for equal gaps between top and bottom tube ends and frame. I am now thinking this is the gaps shown below. (floating)

image.png.7e00f1bfc22674bb2497ab0a72cb68c4.png

I noticed when I started this project there was not gap at the top but did not know enough to question that.

image.png.52fdeef80d8e8a98aa70ef9fd488ec23.png

Am I correct that this is a problem?

Thanks to everyone reading this.

Link to comment
Share on other sites

When a newbie starts to put His fingers in a clock movement, if the clock starts to tick, then the newbie's heart is full of joy, He is inpatient and wakes at night to check if the clock is still ticking... A ticking clock or watch is like a man that breaths and has pulse. And this doesn't mean that that man is healthy and able to do work. The same with the clock - if it ticks and even to the end of power reserve, this still means nothing and doesn't guarantee timekeeping at all. And the main parameter of a clock or watch health is the amplitude. As You didn't mention anything about amplitude, I guessed that it may be You case too...

Yes, the amplitude is measured by degrees of rotation of the balance wheel against it's 'zero' or neutral position. And a table with the amplitude will have one additional column, for the amplitude. Actually, I don't need this table, but just to know if the amplitude is good enough or bad, at least when the main spring is fully wound. Good will mean above 250 degr., and all less than 180 will mean too bad.

Yes, the guard pin and safety roller are what is shown and they would never touch when the balance swings. If they touch, this leads to friction and amplitude loss.

Yes, the gap with the arrow is 0 and it is a real problem, but it is true only when the string is in horizontal position, and I believe that the picture has been taken exactly in such position. In vertical position, which is normal for the balance, the mass of the balance wheel must straighten the hairspring in a manner that the balance will hang on the spring and neither the bottom of the tube, nor it's top will touch the limits. This is easy to check - try to lift or lower the balance along the string and You must see that it is possible and actually it hangs on the spring...

As I understand, You didn't disassemble the movement and cleaned it in whole. No, this is wrong, as all the abrasive particles that got in the bearings with the dust and as wear product will stay there, and the old hardened oil can not be fully removed. The main springs can not be cleaned at all this way too. Sometimes such cleaning leads to stop of the movement again in about one month, and sometimes leads to very fast wear of the bearings.

  • Like 1
Link to comment
Share on other sites

nevenbekriev-

You nailed it with your description of me and my reaction when the clock started ticking again. I am a newbie.  I love the sound and idea of mechanical clocks but the idea of owning one and trying to keep them running has never appealed to me. My wife bought this one and an antique German wall clock.  When I looked into having someone repair them for me, the universal response was "it's really expensive to work on them, you should just replace the movement". So, I had nothing to lose, I started researching them and opened them up. The wife is happy because she hears the sound of the clocks again. But I have gone down the "accuracy" rabbit hole.

In the vertical position, the balance wheel was not floating. It was sitting on the bottom of the frame. I adjusted the lower spring collet and got it floating. It easily passed the 270 degree 3 to 5 minute oscillation test. It took 8 minutes for the wheel to completely stop moving. 

I put it the unit back in the movement and checked the safety pin. It does not touch the safety roller anywhere in +/-270 degrees rotation from neutral position.

But the amplitude of the rotation with the spring fully wound is weak based on what you are saying. It rotates +/-90 degrees from the neutral position. 

No, I did not take the movement completely apart.  That seemed way outside my skill set at the time. There is a reason I became an electrical engineer and not a mechanical engineer. I am much more comfortable with moving electrons than tiny moving metal parts. Will I do it in the long run? Anything can happen. I don't seem to be able to let it go.

  • Like 1
Link to comment
Share on other sites

  • 2 weeks later...

An update. After getting the balance wheel floating correctly and passing the 270 degree 3 to 5 minute oscillation test, I monitored the speed/accuracy for 5 more days. It gained 20 to 25 sec every 24 hours each of the 5 days. That is a big change from prior to getting the balance wheel floating. The speed is now consistent, although too fast. The bad news is the speed control on the balance wheel is already set to minimum. So I don't have any easy way to correct it. 

Also, 2.5 days into the 5 day period, I decided to record a video of the balance wheel and escapement to analyze at slow speed (frame by frame). Prior to starting the 5 day test period, I thought the amplitude was only 180 degrees. But when I viewed the video 2.5 days later, I was getting a full 360 degree amplitude. Not sure if my initial naked eye interpretation of the amplitude was wrong or if it really did increase over time. After winding, I get an amplitude of just under 1 1/4 turns.

The lever pin engagement with the pallets on the escapement wheel looks just fine. They are landing in the lock section of the pallets cleanly.

Not sure where I am going from here.

Link to comment
Share on other sites

Why don't You show the video that You recorded?

Amplitude can not be more than 350 degr, as the rotation of the balance is limited. You rather have 180 than 360. But You have good inprovement.

If the balance is set to max moment of inertia and still the clock is faster, this should be because someone has changed/modified something in balance itself. The fact that the balance was not floating points to such thought. But it is possible to do something - put small equal weights (e.g. small watch screws...) in two opposite holes on the rim. Then 'floating' can change a little, so new adjustment of it must be done

Link to comment
Share on other sites

I wanted to attach the video but It does not appear the forum allows videos. Just still photos. 

Note the excerpts from Daivd Robertson's Document

image.png.a7d4ffb91639617d0e993c3599439fc4.png

 

image.png.72d8484b839bf136776d26cd3952f901.png

I currently meet these criteria. 

I know I can add weights. I just don't know where to get them yet. I have been looking for a reasonably priced used/broken one to take them from.

image.png.ae8b16d9de3033a4f348607f7fede195.png

Thanks again for your thoughts on this. It helps me think through this process.

Link to comment
Share on other sites

Join the conversation

You can post now and register later. If you have an account, sign in now to post with your account.
Note: Your post will require moderator approval before it will be visible.

Guest
Reply to this topic...

×   Pasted as rich text.   Restore formatting

  Only 75 emoji are allowed.

×   Your link has been automatically embedded.   Display as a link instead

×   Your previous content has been restored.   Clear editor

×   You cannot paste images directly. Upload or insert images from URL.



  • Recently Browsing

    • No registered users viewing this page.
  • Topics

  • Posts

    • yes I noticed the new site and I miss the old site. It's the unfortunate problem of the Internet here today gone tomorrow sometimes some of the stuff gets backed up and sometimes well it does not then the problem with the early Seiko's were there were not necessarily designed for distribution across the planet and as such there is no customer support for them. So trying to find early stuff like technical information or sometimes even parts list for older Seiko is is problematic. But I did find you a you tube video. A quick look he seems to take a heck of a lot of time to actually get to the service single I did not watch all that but it does look like he did disassemble or started to say there's a tiny bit here  
    • RichardHarris123: Hello and welcome from Leeds, England.  I have family all over Australia, went as £10 poms Thanks Richard. Hope you’re able to visit your family here and that they’ve all done well 🙂 My relatives arrived from England in the 1790s transported on the ‘Second & Third Fleets’—a story of timber sailing ships, of convicts and doing well in this huge Country of Australia. When I visited the UK in the 1980s, I was too young to comprehend the depth and breadth of its history…  Best wishes, Mike William Chapman, my 4th great Grandad’s charges, at age 23 read at the Old Bailey; sentenced to 7 years of transportation to Sydney.
    • The whole process and the progress are closely observed, it's hand-driven and very controlled. I can't see the "danger", unless you are watching the TV while doing it. As you could have read, and in this quote "wheel" is the balance-wheel.
    • Have you got the pallet fork installed in the movement when you see the train move when using the setting works? As nevenbekriev said, without the pallet fork to lock the train, the behaviour you are describing is normal. If this is happening with the pallet fork installed, you have a problem in the gear train, it should be immobile when the pallet fork is locking the escape wheel.  The fit of the circlip above the pinions on that wheel is crooked in your pictures, it should sit flat up against the upper pinion as in Marc’s picture.  Hope that helps, Mark
    • Hi I got a Jaeger LeCoultre K911 movement, where one of the stems was broken. Part no. Should be 401.  Im based in Europe and tried Cousins but its discontinued. They except to get stem in stock for cal. K916 but will that work? Or Is there a way out to join the ends?
×
×
  • Create New...