Jump to content

Making a New Balance Staff


Recommended Posts

I am making a new balance staff for an 18S Waltham. I think the balance is friction fit, however, my first cut 1.45mm was a bit too much and the balance fits but is not tight enough. I decided to leave a little lip so I can rivet it on as well (let's see how that goes:).19e641063037bdccd4915a9b3d110fc7.jpg

I then cut the hairspring part at 0.9mm and the pivot at 0.12mm; cut down to 0.2 and then reduced using a stone.340ec79722a14ba5793dcd25aded4cb4.jpg794b88d4633f64a93536885f947df1ee.jpg80cfa1740f9d9242fc38592996abddd7.jpg

I had to move the Steel Rod out as I had worked my way in too far with a failed first cut on the balance part. I then cut the roller table side and angled the largest diameter.cc224b5f9b19d0b548f1af438af261ca.jpg8f83637792b552e627499582f0045006.jpg353a66b0a9a69378452144001703a7b3.jpgb739e131bc6529a6b6c0a4698a2f3f5e.jpg

Tonight I cut the lower pivot.

 

 

Sent from my iPhone using Tapatalk Pro

  • Like 5
  • Thanks 1
Link to comment
Share on other sites

jdrichard, I've moved this thread to the appropriate section, please take the time to select when posting.
 

Sorry about that. Started off with the intent of just saying stuff and then got specific :)


Sent from my iPhone using Tapatalk Pro
  • Thanks 1
Link to comment
Share on other sites

Started cutting the bottom half of the stafffec3613fb1100133e6e509c36b76e017.jpgSized it against the original staffc8a4492c730fc047eb29e7b88831d1c5.jpgGraved it down to about 0.2 mm and then filed it down to size with a stone and oilc369a124f40a38fc5b14b4984a5e5766.jpgI then burnished itb938e4b2a0378ff62ed3b0f0ea299ec0.jpgThen i fitted the roller table to make sure the staff was the right size.f1228ce2ea5a7e4252a066f31e7168fd.jpgI then fitted the staf on its own in the movement to make sure the length was right and the 0.12 staff pivots fit into the upper and lower jewel. It was a little long so I mounted the staff in the lathe and tool a little off the top pivot.71f0378de6a5961a141be31dba7ca514.jpgI compared the two staffs2cdc381c778e45725efca60c783038f9.jpgI Then fit on the staff loosely and assembled the unit as a final check prior to staking on the staff.49133bd18092ccb9a57444c144413c4e.jpg0cc8729d462c861f793c94f9a3a856ad.jpgAll done for now. Tomorrow I stake on the staff and roller table and test again.


Sent from my iPhone using Tapatalk Pro

  • Like 2
Link to comment
Share on other sites

Finishing the staff and riveting on the balanceccb956c1a1b284fdeae1a36950b31190.jpgUsing the Jacot, trimmed a pivot down and burnished themfc17dc9a5a77c2386c7fcb7fcd784885.jpgLower pivot was still to wide so put it back in the lathe to stone it down to size.5bd036f83b780a3b612387648d684737.jpgAligned the Hairspring and punched it on.c4060ab491d1fd7f9cbfa195aa6b04aa.jpgb7f677328e37ff432c840ab7f8dd891d.jpgIt was complete and completed the install. Watch is currently running down with the new balance. Will completely disassemble and clean and oil and reassemble. DONE:)684a98a8be11c2dbbd8069dbb6f9cd07.jpg


Sent from my iPhone using Tapatalk Pro

  • Like 3
Link to comment
Share on other sites

Making a friction fit balance staff on a lathe is very tricky. As I was cutting a staff for a waltham, i took a little too much material off and the staff was not fitting completely snug.a9d69f9bd5de64ab6d13188f29501b25.jpg

So, i decided to leave a little lip so i could river it on.60ac02be4788ca27d6a060025354ec66.jpgd7700e74ead1db77bfff7dec29a34f7a.jpg

 

 

Sent from my iPhone using Tapatalk Pro

  • Like 1
Link to comment
Share on other sites

  • 1 month later...


  • Recently Browsing

    • No registered users viewing this page.
  • Topics

  • Posts

    • Here is the insert ring for rectangular or elliptical movements: Note that the length is the side with the stem cut out on the spreadsheet (in the picture below this is 15.15: Here is the fake pdf file, again you need to convert to .zip after download to access the FreeCAD and 3mf files. Rectangular insert disc.pdf    
    • as you took the mainspring out what did it look like? It's amazing how much amplitude you can get if the mainspring actually has the proper shape. last week I was doing a 12 size Hamilton and was very much surprised with the beautiful back curvature the mainspring had. Then the watch had a really nice amplitude the group would be so proud it was 350 until I dropped the lift angle down to 38 that drop the amplitude quite a bit below 300. then with the beautiful back curve it still had really nice amplitude the next day. I really wish all my mainspring's look like this as the watch had beautiful amplitude the next day. So many of the aftermarket pocketwatch Springs I see now do not have anything resembling a back curve may be a slight curve and that's about all. They still work but they just don't work as nice as a properly made spring. then Omega as all sorts of nifty technical documentation unfortunately every single corner is watermarked with where it came from who downloaded it etc. very paranoid company. On the other hand I will snip out images like from the document on recycling a mainspring barrel. for instance here's the section on what your mainspring should look like. water damaged a lot of times means rust was there rust on this watch?
    • I dont understand why a patreon membership would have limited places ??
    • Welcome to the forum, enjoy. It’s highly unlikely you will be able to purchase a new bezel look on eBay for a pulsar watch for repair to find a bezel.
×
×
  • Create New...