Jump to content

Leaderboard

Popular Content

Showing content with the highest reputation on 07/13/18 in all areas

  1. I just finished repairing a Hamilton #940 21j open face 18size P/W. made in 1909 I have been working on it as I get the parts needed. I cleaned it , replaced the mainspring, balance staff, pallet jewels, top balance stone , and crystal . I had a bit of trouble with the timing , but finally got it to 20 seconds a day, which I can live with. While doing that I finished a painting for an up coming show called "Kathleen Louise Passing Bald Head " So I'm happy today
    2 points
  2. One other part I made on the "new" lathe is a proper strong and deep enough die to deal with tall crystals such as on the 1680 and VERY tall one of the 1655 (Sea-Dweller). Most foul on the crystal. My old solution was a 30mm 12-point socket. it works, but it does not press the retainer flat and square relative to the case top surface, so I have to go back and "peck" it down with another tool all around the crystal... Here it is: (The blue Tudor will be it's first victim)
    1 point
  3. Hey guys. Been occupied by other things lathely, namely getting an old lathe up and running here at work... It's quite beat and abused but Its a high quality Hardinge lathe. I rebuilt the compound (which clips onto the dovetail way as it's a lower-end second-operation lathe) so it has limited travel. The angle scale (which is under the top of the compound and visible through a magnifying glass built in) was completely covered in rust and grease. Now it's visible... It came in handy to set ~2 degrees of taper for my tack! I also took the excessive lash out of the compound ways so they are nice and tight now. This is a sweet lathe with a 3-jaw chuck as well as an assortment of 5C collets. I learned from a master tool and die maker on the high end version of this- the tool room lathe, with a proper apron able to cut inch and metric threads. This is it's lesser cousin. A brass rod was tapered as thin as I could and then finished with sand paper as it was deflecting from the tool of course and not cutting as it got thin... I pressed it into a 1" slug of aluminum. A bit of tubing to keep it safe and a recycled container and we are done! Anyway, here's the tack:
    1 point
  4. Try Omega chrono sub hands. Like the 821 caliber (or 321 but those get silly expensive) I used an Omega running seconds sub dial hand (the left one) on an a Valjoux 7734 that worked perfectly. The minute counter (right sub dial) needs to be broached slightly. Check at www.ofrei.com as I believe they list the diameters of the pinions of the hands in most cases.
    1 point
  5. Glad you got it all sorted out! When first reading, I was going to suggest wrapping dental floss around the canon and then trying. Looks like you found a good one! Just clean and polish so it gleams like new for next time!
    1 point
  6. Very attractive watch. I like shiny pretty things. Sent from my iPhone using Tapatalk
    1 point
×
×
  • Create New...